Process innovation at the Sandy lumber mill.
Metlen, Scott ; Lawrence, John J.
CASE DESCRIPTION
The primary subject matter of this case concerns the value of
quality control and continual system improvement. Secondary issues
examined include project implementation, and quality management issues.
The case has a difficulty level appropriate for undergraduate seniors
towards the end of a semester quality management class and for graduate
students. The concepts presented in the class are not trivial and
several hours during class can easily be used to discuss all issues. A
student's degree of understanding of process control issues,
financial analysis, and quality management issues dictate the amount of
time out of class each will spend to address case issues. Most students
will need to spend a minimum of four hours to address all issues.
CASE SYNOPSIS
The Sandy sawmill produced dimensional lumber. The mill had
recently completed a $2.6 million process upgrade that had allowed it to
improve yields and better match lumber produced to market conditions.
Revenues had increased from $29,000,000 to over $40,000,000 as a result.
But challenges and opportunities remained. The milling process was
theoretically capable of producing closer to specification, and
operators still had difficulty identifying where in the process defects
originated. Further, the mill manager was somewhat overwhelmed by the
amount of data being produced and how best to use this data. The case
ends with the mill manager wondering what he should do next to get the
most out of the new system. This case was designed for use in a quality
management class to facilitate discussion of the design and
implementation of a statistical process control systems.
INTRODUCTION
Tony Flagor watched the computer screen display real time
information on the boards being processed at the Sandy Saw Mill and
marveled at the new control process now in place. He was proud of the
changes that he and his team had made. Nevertheless, even though the new
control process was vastly superior to the one that had been in place
when Tony had first become mill manager, it still did not seem to be
adequate. The milling process consisted of many steps, each one
representing a unique opportunity for a quality problem. Unfortunately,
the control process did not display which task caused an out of
specification board, only that a given place on a given board did not
meet specifications. Furthermore, the measurement system in place had
the potential of creating an unfathomable number of data points per
minute, and Tony was unsure how best to use all of that potential data.
What Tony did know was that he needed to continuously improve the
effectiveness of the mill in order to stay competitive, and he believed
that effective real time process control was key.
The US lumber industry in which the Sandy Mill competed was highly
competitive, and generating profits had become an increasingly
challenging task for everyone in the industry. An 18% increase in lumber
imports from 1997 to 2002 (Kelly, 2003) and increased effectiveness of
processing technology had created a situation of high supply relative to
demand despite diminished supplies of raw material due to closure of
many national forests to logging to protect endangered species. From
1997 to 2003, 117 (14%) of the 829 United States softwood lumber mills
went out of business (Spelter, 2003) and the number of trees harvested
declined by 6.85% (United Nations Economic Commission for Europe, 2003),
yet lumber production in the USA was static for the same time period
(Kelly, 2003). The surviving operations had to increase effectiveness
(extract more boards of higher value from a given log at lower operating
costs) and gain economies of scale to stay in business. The Sandy lumber
mill was a mill that so far had been successful in increasing lumber
production effectiveness.
The mill manager in charge of milling operations and milling
improvements at the Sandy mill was Tony Flagor. Tony came to the Sandy
mill from a career in the Navy as an electrician where his
responsibilities included electrical maintenance and training. After the
Navy, Tony earned a BS and MBA from the University of Washington.
Tony's first job at the Sandy mill was as maintenance manager after
first working for one year as an electrician in an adjacent plywood mill, which was also owned by the company that owned the Sandy mill. The
position of maintenance manager was for both the Sandy mill and the
plywood mill. Within a year of taking the maintenance manager position,
Tony applied for the mill manager position at the Sandy lumber mill.
Much to the surprise and anger of some longtime employees of Sandy who
had also applied for the same position, Tony became the new manager of
Sandy. There were many reasons Tony was selected for the position. His
personal work ethic and ability to work with everyone but still make and
enforce tough yet fair decisions regarding subordinates enabled Tony to
have productive work centers. As important as Tony's human resource
ability was in management's decision to make Tony the new manager
of Sandy, it was Tony's willingness and ability to incorporate new
technology into the milling processes that cinched management's
decision.
Under Tony's direction, the Sandy mill undertook and
accomplished a massive process redesign, which allowed the mill to
increase the level of profits it generated for its parent company. Tony
was pleased with the new processes because they were consistent with the
strategic direction of the parent company, which involved focusing on
those business units that had and could maintain a competitive advantage
and that had potential to grow. Despite the success of the new process,
Tony knew that the competition was not resting and that he would have to
keep improving process effectiveness in the most cost effective manner
possible to maintain and strengthen the competitive advantage that the
mill currently had. Toward that end, Tony had to decide what the next
step was to continue to improve the effectiveness of the mill.
COMPANY BACKGROUND
The parent company of Sandy was founded in the early 1900s. The
company was a vertically integrated, diversified forest product company
that owned 1.5 million acres of timbered land and operated 15 mills. The
mills included lumber mills such as the Sandy mill, paper mills,
particle-board mills, oriented strand board mills, and plywood mills.
The Sandy mill was a softwood lumber mill that had been in
operation since 1972. It was nonunion, paid above industry average wages
(one person year did cost the company an average of $50,000.00), and had
the capacity of producing 85,000,000 board feet per year from logs
ranging from five inches to 18 inches in diameter and eight to 18 feet
long. Unlike many current mills, Sandy was expected to create lumber
from multiple species of trees; Douglas, Alpine, and White Fir,
Engelmann Spruce, Cedar, and, Lodge Pole Pine. To take advantage of this
expected flexibility, the milling process required a greater amount of
operator knowledge because mill operators had to understand the
peculiarities of production inherent to each species. True flexibility
also required a process that had fast, easy setups so that operators
could quickly start processing of a different species to meet dynamic
market demand. Up until 2002, the mill had an efficiency driven
production process where the focus was only on making as much lumber as
possible as cheaply as possible. Mill managers paid less attention to
what species and dimension was currently in demand in the marketplace,
but rather focused on how to get the longest production run for a given
species. This efficiency focus was driven by the nature of the process
in use at that time.
MILLING PROCESS, PRE-2002
The milling process as of 2002 consisted of a traditional lumber
mill process that was labor intensive (Exhibit 1). The mill produced an
average of 85,000 million board feet (MMBF) (one MMBF equals1000 board
feet) of dimensional lumber per year. A board foot is a metric used in
the lumber business measuring 1 inch x 12 inches x 12 inches and
dimensional lumber refers to the width and depth of the boards produced.
The original mill produced 2" X 4", 2" X 6", 1"
X 4", and 1" x 6" dimensional lumber. To simplify
calculations, all boards in this case will be assumed to be 2" X
4" where one lineal foot equals .67 board feet and the average
board is 14 feet long. The mill operated 202 days per year with two,
ten-hour shifts per day. The lumber produced sold at an average selling
price of $347 per 1000 board feet (m.bd.ft) or one MMBF.
The start of the process consisted of a sawyer on a log carriage.
The sawyer would quickly inspect a log and with partial help from a
computer decide how the log should be cut to get the most lumber the
quickest. The lumber the sawyer made would proceed by conveyor belt to
inspectors who would sort the lumber by dimension, length, width, and
depth (see exhibit 1 for a schematic of the process). Seventeen people
per shift were involved in the total process; most making many
qualitative decisions that would affect the quality and volume of
process output. To help make these decisions more accurate and easier,
and to keep all workers busy, large batch sizes of uniform logs of one
species were the norm. Thus, to produce the volume of output needed, the
mill often produced lumber from certain species and in certain
dimensions that had lower market value relative to lumber with other
dimensions or from other species in the interest of achieving higher
milling efficiency and output. This practice created a focus on
efficiency, not market effectiveness.
In addition to the focus problem created by the perceived need to
produce large batch sizes effectuated by a labor-intensive process,
lumber quality and yield per unit of raw material (a log) suffered.
Although the process operators were experienced and good at the tasks
they performed, the shear number of decisions made daily, tight
dimensional market specifications required to meet lumber standards, the
physically demanding and tedious nature of the work, and a large number
of shifting process variables created a situation where many units of
output were out of specification. The same problems also generated
faulty decisions regarding the best way to get the most lumber out of a
log, which in turn lowered the number of board feet of lumber produced
relative to the board feet encompassed within each log. Not only was the
board foot yield affected by sawyers' decisions, but the total
dollar value per time of operation was also influenced negatively
because the sawyer concentrated on dimensions that more easily derived
the most volume of lumber the fastest, not the greatest amount of
dollars.
The mill's efforts to control quality during the production
process consisted of having personnel measure eight boards in eight
places within the first 10 minutes of start up to see if production was
within specifications. The focus was on whether the process was
producing boards within process specification at start up, as opposed to
whether the process was in or out of control in real time. Real time
process adjustment decisions were seldom made based on the direct output
from the QC process after start up. Process decisions made by operators
were primarily a function of their tacit knowledge of the inherent
variability embedded in the process system, and how that variability
affected outcomes.
Required lumber dimensions were determined by industry standards
(i.e., a dried two by four needed to be a minimum of 1.50" deep and
3.50" wide), and the mill experienced increased costs as a result
of being either under or over these dimensions. The more costly problem
was being under specification. Product that was under specifications had
to be sold on a secondary market at a significant discount. Tony
estimated that being under specification cost $20.00/1000 board feet,
which could cost the company up to $8,000.00 per day in lost profit if
the entire production for the day was under specification. Because of
the high cost of being under specification, the process was routinely
set to overcut .350" (Standard deviation (SD) .11) over market
specification for width and .210" (SD .075) for depth. Of this
overcut, however, .006 inches was necessary for shrinkage during the
drying process to reduce the moisture content of the wood to 12-16% and
another .015" was necessary to allow for variation in saw kerf (width of the cut made by the saw that is a representation of the output
of the saw sharpening process). The remainder of the overcut was to
protect against the possibility of producing output that was under
specification due to other system variability. With the mean overcut
listed above it was felt that the milling process would produce few
boards under market specification due to the normal variability of the
system. Tony was not sure what the long run average variability of the
system was exactly, but knew that the theoretical minimum variability
was the variability associated with variation in kerf.
Cutting product that was over specification did not impact the
product in the marketplace as any boards that were produced over
specification were corrected in the final planing process after the
green lumber (the term green here is the term used in the industry to
describe lumber that has not yet been dried) had been dried. Cutting the
lumber over specifications did waste material, however. Tony estimated
that every 1/1000 of an inch cut over market specification on both width
and depth dimensions together cost the company $20,302.00 per year in
wasted wood. The plant tended to operate with a bias toward avoiding
undersized lumber, and oversize system drift was seldom caught or
worried about and at times whole shifts would produce boards that
exceeded the targeted overcut.
PLANNING FOR CHANGE
When Tony took over as manager the board feet of lumber produced as
a percent of the number of true board feet of logs introduced into the
production process was 85%. Even though the mill was making money,
industry competition was eroding profits. Tony knew he had to create a
production process that increased yield by producing more boards per log
by reducing the overcut and optimizing the cut decisions based on both
number of board feet and market value per board foot for a given log. To
accomplish the yield and market value increase, the number of human
decisions had to decrease, and an effective QC program had to be
implemented. An effective QC program would give operators the necessary
ability to manage board dimension in real time given the need for
narrower process settings to produce boards closer to market
specification.
Tony knew that changing the process would be challenging from a
human resource perspective. The mill was located in a small town and was
operated by people with little education beyond high school. Up to three
generations of some families worked at the mill at any one time, and
traditional milling practices were revered. Due to this reverence for
traditional practices and the low level of education, workers were going
to be particularly suspicious of the new technologies that Tony knew
were necessary to keep the mill competitive.
When Tony became sawmill manager he held a meeting with the
mill's employees to explain why the traditional milling process was
no longer adequate and to explain that the process and the way operators
managed the process would have to change if the mill was to remain
competitive. Process improvement had to happen in all areas of the
milling system or everyone would be out of a job. The targets Tony gave
were to reduce the average board overcut by .06" for width and
.054" for depth, increase the board feet of lumber recovered to
true log board feet bought to 95%, and to increase the per thousand
value a minimum of $30/1000 by cutting to market demand. Then Tony did
something the employees were not used to--he asked them how they thought
they should proceed and promised there would be no lay offs from the
company due to process change. After numerous meetings between Tony and
his employees and Tony and his managers, everyone agreed that the
current processing system was no longer adequate. The process operators
were expert, dedicated employees who were limited by the current process
in how much product they could produce and the quality of that product.
Thus, it was agreed that the mill employees needed to design and
implement a completely new, automated process utilizing the latest
technology if the Sandy mill was to stay in business for the long term.
NEW MILLING PROCESS
During 2002 and part of 2003, under Tony's leadership, Tony,
his employees, and equipment suppliers/consultants installed an
automated milling system that they had designed (Exhibit 2). The system
consisted of two major components: (i) a full log scanner and the
corresponding software and controls to allow computer optimized canter
saw cuts; and (ii) new scanners for the board edger and trim saws and
the corresponding software and controls to allow for computer optimized
trimming of the individual boards produced. The new system also include
a new method of saw maintenance that reduced the saw kerf from .135
inches to .115" and the SD of the kerf from .005" to
.002". Exhibit 2 provides a process flow diagram of the new system.
This original installation cost $2.6 million and was completed
within the time specified, but it was a stressful time for the
organization. To help reduce stress and keep employee buy in, management
provided extensive training to the process operators so that they could
not only operate the new milling system, but also understand the
technology that enabled the system. Further, as promised, the management
at the Sandy mill did not lay off any employees due to the new system,
although one employee was reassigned to another job within the company.
Tony made sure he took time to ski, bike, and spend time with his family
during this time as a way to cope with the stress, and he encouraged his
employees to also maintain balance in their lives.
The new system improved log yield to 95% and helped the mill become
more market driven as the decisions on how to cut the logs and boards
was transferred from operators to sophisticated computer software. The
decision rule the computer followed was based on the size and quality of
a log, and the dimensions that were in demand and had the highest prices
in the marketplace. While the mill still operated the same number of
hours as before, production increased from 85,000 MMBF to 116,500 MMBF.
Some of the increased production was due to an increased speed of
production (as a result of faster decisions) and some due to less waste
(as a result of better decisions). Further, completely automating the
sawing task helped reduce setup times and enabled shorter batches by
species and made it practical to have a greater mix of log sizes within
a species batch and still realize the optimal number of board feet of
lumber relative to the board feet in a log. The ability to run smaller
batches and to optimize the amount of lumber based on the value of
specific dimensions increased the average selling price per thousand by
$25/MMBF.
One disappointment that the team experienced with the initial
installation was the team's inability to meet its targeted
reduction in overcut. The team was able to reduce the overcut by .03
inches (.320" width, .18" depth overcut, SD .099" width,
.059" depth), but this was only about half of what was targeted.
The primary limitation was that the initial install did not provide a
feedback mechanism such that the production system could be monitored
for board dimensions on a real time basis. The scanners used at the trim
saw and the board edger could have been used for this purpose, but the
software was not designed to do so and would have been expensive to
convert. The trim scanner inspected a board to determine the optimal
length or lengths to make that board determined by defects within the
board and original length of the board. Standard lengths ranged from
eight feet to 20 feet in two-foot increments. For example, a 19 foot,
defect-free board could be made into an 18 foot board, an eight and ten
foot board, or two eight foot boards. Market price would dictate the
optimal decision. If there were a defective spot on the board, the
algorithm used in the computer software would determine how to cut the
spot out and still produce a valuable board or boards. Similarly, the
scanner for the edger inspected the rough boards that had round edges to
determine the optimal width of the board that would remove the round
edges from the board. About 1/3 of production went through the edger and
all production ultimately passed through the trimmer operation. Both of
these devices essentially took a digitized picture of a board where 95%
of the measurement error will range between +/- .008". The scanner
software was not designed to capture and consolidate this data, however,
so even though the original install did achieve less waste by making
better decisions about the width and length of a board to make, it did
not include an easy method of determining real time status of the
production system.
NEW QUALITY CONTROL PROCESSES
To achieve real time system status so machine settings could be set
tighter, Tony immediately had two additional scanners placed in the
system shortly after the initial system install. These scanners just
monitored board thickness and width, and were accurate to +/- .002"
when the lenses were clean. The first scanner was placed in the process
just after all the boards from both sets of vertical band saws were cut
to the optimal width. The second scanner was placed in the system
following the trim task where all boards going through the system were
cut to optimal length/s (see Exhibit 2). Each scanner could scan 1000
measures per second on boards that were being conveyed at approximately
700 feet per minute thus, the QC system had the ability to measure all
boards in both width and depth dimensions every 1/8 of and inch. This
represented an incredible amount of data that Tony was still trying to
figure out how best to use. Due to the nature of the current process,
however, it was not possible to tell which board came from which band
saw on the first scanner, or which board came from the band saws or the
gang saws or which saw on the gang saws on the second scanner.
The data from each scanner was graphed in real time against
targeted process specifications and was used in an Engineering Process
Control (EPC) protocol. When 5 out of 10 boards, 30 out of 100 boards,
or 50 out of 300 boards were above or below the process specifications,
the computer alerted the operators. Once alerted, the operators
determined and fixed the problem that was causing boards to be produced
beyond process specification. Because operators had no way to tell how
the out of specification board came through the system from the
displayed data, the system could not be shut down until the operator
determined the problem. There were at least 12 different places in the
total system where adjustments could change, and out of specification
boards would be produced as a consequence. At the production rate of one
board per second, if all 12 areas were producing under size boards, 8333
board feet with a $20 penalty per MMBF could be made in the ten minutes
it usually took the operators to find the problem.
In addition to the computer-generated alerts that the operators
received from the system, the production supervisors had continuous
access to the real time graphical process output that the system
generated in the mill's control room. Tony had yet to establish a
clear protocol on how supervisors should make use of this graphical
output. Sometimes supervisors noticed system drift or patterns evident
in the graphical output and took action prior to any alert being
generated by the system. Further, sometimes supervisors took action to
make a correction when the amount of overcut moved higher than the
established overcut target. Other times, Tony was not even sure if
supervisors looked at the output except at the end of the shift. Tony
also recognized that the data being generated by the system provided the
potential to evaluate the effectiveness of a given run or shift. Tony
was unsure about the wisdom of using the data for such purposes and how
best to understand the causes of the variations he saw in the data
within a given shift and between different shifts.
The addition of the two scanners to the system allowed the overcut
to be reduced to .290" (SD .09") for width and .156" (SD
.05") for depth because of the reduced standard deviations of
overcut. The mill continued to follow the EPC protocol described above,
and this protocol resulted in the system being shut down at least four
times on a typical day to adjust at least two of the 12 adjustable areas
each shut down. Unfortunately, the new QC system did not provide a
method of determining where the out of specification boards were
processed in the system (such a system would cost approximately
$10,000.00), nor was the software set to determine what part of the
board was out of specification (such software would also cost
approximately $10,000.00).
Knowing what route a specific board came through the production
system would allow the system to be shut down as soon as a problem was
detected because an operator would know which of the 12 areas was
creating the problem. Knowing which part or parts of the board was/were
out of specification would also provide clues as to what the problem at
a specific area might be. Tony knew that the causes of some problems
were so certain that automatic adjustments could probably be designed
into the system such that the system could make the necessary
corrections before the operator was even aware there was a problem. Tony
knew of several locations in the process where such automated
adjustments could be designed in and assumed that with the help of mill
operators, all twelve areas of adjustment could be automated. Tony
estimated that it would cost between $5,000 and $15,000 per location for
automated adjustments. Tony expected that if these instruments were put
in place in conjunction with knowing immediately where an out of
specification board came from, the average overcut could be reduced
another .06" (SD reduced further to .057") for width and
.02" (SD reduced further to .026") for depth.
WHAT NEXT
Tony and the sawmill operators were pleased with many of the
outcomes produced by the new process system, but knew they had to keep
improving the process. Because operators could not react fast enough
when the system started producing product out of specification, the
amount of deliberate overcut was still large relative to the lower bound
of milling system variation embedded in the flex of the saw blades. The
QC system was producing massive amounts of data, but the operators did
not seem able to utilize the information to produce boards closer to
market specification, nor were the operators able to determine the
source of specification problems from data alone. Tony knew that he had
to revamp the QC system, preferably so that the milling process system
would adjust automatically to information produced from the QC system.
However, Tony was worried that upper management might balk at putting
more money into the QC system and that the milling process operators
might not understand a more sophisticated QC system and not be able to
take advantage of all the possibilities for milling system improvement
and control. Tony now had to decide whether or not to make further
improvements in the QC system, keeping in mind the significant cost of
such changes and the capabilities of his operators to utilize a more
advanced system effectively.
[ILLUSTRATION OMITTED]
Task descriptions pre 2002.
Task 1, Debarker: The first step is to remove the bark from the
log. The bark is used to generate steam for other milling processes.
Task 2, Mark II Canter Saw: The log is cut into a certain sized
rectangle by removing slabs from the log that are a given thickness
depending on the dimension of board required and the initial log
dimensions. This task is critical in determining the board feet of
lumber salvaged from a log. If the first cut is made in the wrong place,
fewer usable boards or boards with lower market value will be produced.
The decision on how to cut each log is made by the sawyer based on a
visual inspection of the log and the help of a decision support system.
Task 3, Gang Saw: The rectangle produced by the Heading Sawyer is
automatically cut into individual boards. The Gang Saw consists of up to
13 horizontal circular saws that have to be precisely set to produce
boards of equal thickness.
Task 4, Hand Sort: boards are sorted by width, thickness, and
approximate length. Boards that are the correct width and thickness are
trimmed to an optimal length and stacked by length to go to the Kiln dryer where the lumber is dried to 12% moisture content from a normal
green condition of 20 to 40% moisture content. Boards that are not the
correct thickness or have too much wane are sent to Task 5.
Task 5, Slap Resaw: boards from the Canter Saw that are too thick
are adjusted to the correct thickness and sent to Task 6.
Task 6, Board Edger: boards from the Slap Resaw are edged to the
correct width and sent to the trim saw.
Task 7, Trim Saw: boards are cut to optimal length and sent to be
stacked by hand for transport to the Kiln.
Task 8, Chipper: wood that cannot be made into lumber is ground
into chips that will be burned to make steam or be used to make paper.
[ILLUSTRATION OMITTED]
Task descriptions post 2002 (with new technology/systems shown in
bold).
Task 1, Debarker: The first step is to remove the bark from the
log. The bark is used to generate steam for other milling processes.
Task 2, Log Scanner: scans are taken of the log using infrared
scanners and the optimal number and thickness of slabs are determined
automatically based on the shape of the log and the value of the lumber.
Task 3, Computer controlled Mark II Canter Saw: The log is cut into
a certain sized rectangle by removing slabs from the log that are a
given thickness depending on the dimension of board required and the
initial log dimensions. This task is critical in determining the board
feet of lumber salvaged from a log. If the first cut is made in the
wrong place, fewer usable boards or boards with lower market value will
be produced. This task is now controlled by a computer and optimal cuts
are made to produce the greatest number of boards with the highest
market value from each log.
Task 4, Gang Saw: The rectangle produced by the Canter Sawyer is
automatically cut into individual boards. The Gang Saw consists of up to
13 horizontal circular says that have to be precisely set to produce
boards of equal thickness.
Task 5, Scanner for Edger: scans using infrared scanners are taken
of the slabs from the Canter Saw to determine automatically what board
or boards can be made from the slab and then the boards are sent to Task
6 where they are edged to the proper width.
Task 6, QC Scanner 1: slabs are measured using infrared scanners to
determine thickness to determine if the Heading Saw blades are set
correctly.
Task 7, Board Edger: boards are edged to the correct thickness.
Task 8, Scanner for Trim Saw: boards are scanned to determine what
optimal length of boards can be made, this information is used after
Task 8 to determine which stack each board is sent to by length.
Task 9, Trim Saw: Boards are cut to optimal lengths and sent to be
stacked for transport to the Kiln. A one to three board solution is
possible.
Task 10, QC Scanner 2: all boards are measured using infrared
scanners to determine width, thickness, and length.
Task 11, Sorting: boards are sorted automatically from information
from Task 8 by length to go to the Kiln dryer where the lumber is dried
to 12% moisture content from a normal green condition of 20 to 40%
moisture content.
REFERENCES
US Census Bureau. (2002). Economic Census. Retrieved May 22, 2004,
from www.census.gov/econ/census02/advance/TABLE2.HTM.
United Nations Economic Commission for Europe. (2003). Timber
Bulletin ECE/TIM/BULL/56/2. Retrieved May 22, 2004, from
http://www.unece.org/trade/timber/database/fps98_02.xls.
Kelly, Thomas, (2003) Lumber Statistics. United States Geological
Survey. Retrieved May 22, 2004, from
http://minerals.usgs.gov/minerals/pubs/of01-006/wood.xls.
Spelter, Henry & Alderman, Matthew (2003). Profile 2003:
Softwood Sawmills in the United States and Canada. United States
Department of Agriculture. Research Paper FPL-RP-608. Retrieved May 22,
2004, from http://www.fpl.fs.fed.us/documnts/fplrp/fplrp608.pdf.
Scott Metlen, University of Idaho
John J. Lawrence, University of Idaho